Monowakari
XS400 Enthusiast
Tore my carbs apart and cleaned them thoroughly with carb cleaner. Set the timing to be fairly accurate and point gap is perfect. Valve clearances all within spec on the tighter side (quite quiet now, might have read my old posts on the valve train noise, has all but gone away now with valves in spec.!!!).
Reassembled with new carb intake boots in prime condition. Idle mixture screw is out 3.5 turns each side, they are fairly synced, going to build a manometer today or soon (this week).
The only thing I couldn't get out in carb rebuild was the pilot jet due to not having a small enough screw driver to get in there but throughly cleaned with carb cleaner with a tiny spray nozzle and just blasted 'er.
You can hear the pods gurgle in air when I engage the throttle and it hesitates for a fraction like its bogging down then it soars to where it should be and no issue through idle at ~1200rpm to revving to 6-7k rpm (in neutral on center stand). You can even see the vacuum action on the clamp or the rubber deflecting underneath it.
All I can think of is, should have cleaned pilot jet but couldn't get it out...can always go back in.
Perhaps the floats need much more accurate adjustment? [It's like 1.05" float height and just under 1-9/32" fuel max (float extended all the way up so just over an inch and a quarter). - basically 26mm and 32mm, juuuuust off...]
Idle mixture screw in or out a bit?
OR this is how it should sound, question is the slight hesitation when engaging throttle... Revs fine and going to take it for a quick test spin around the block as I'm sure all is in running order...
Cant wait for Pamco with electronic advancer to arrive, will probably help alot, and manometer adjustments.
Anyways, thanks fellas, this is the best forum I've ever been on!
Reassembled with new carb intake boots in prime condition. Idle mixture screw is out 3.5 turns each side, they are fairly synced, going to build a manometer today or soon (this week).
The only thing I couldn't get out in carb rebuild was the pilot jet due to not having a small enough screw driver to get in there but throughly cleaned with carb cleaner with a tiny spray nozzle and just blasted 'er.
You can hear the pods gurgle in air when I engage the throttle and it hesitates for a fraction like its bogging down then it soars to where it should be and no issue through idle at ~1200rpm to revving to 6-7k rpm (in neutral on center stand). You can even see the vacuum action on the clamp or the rubber deflecting underneath it.
All I can think of is, should have cleaned pilot jet but couldn't get it out...can always go back in.
Perhaps the floats need much more accurate adjustment? [It's like 1.05" float height and just under 1-9/32" fuel max (float extended all the way up so just over an inch and a quarter). - basically 26mm and 32mm, juuuuust off...]
Idle mixture screw in or out a bit?
OR this is how it should sound, question is the slight hesitation when engaging throttle... Revs fine and going to take it for a quick test spin around the block as I'm sure all is in running order...
Cant wait for Pamco with electronic advancer to arrive, will probably help alot, and manometer adjustments.
Anyways, thanks fellas, this is the best forum I've ever been on!
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